hello!
I've been having some guiding issues with my CEM 70 so I thought I'd share my findings here maybe someone can give me an insight for what might be going wrong.
Basically, the main issue with the mount is instability; I get acceptable guiding on some nights with stable values between 0.4 and 0.6"/px (very smooth curves) and bad guiding on most other nights with RA peaks. My first reasoning was seeing conditions but I have some reasons to believe it might be mount mechanics or PHD2 settings.
Before I delve into the details, I've tried:
- different balancing techniques
- all possible guide settings in PHD2 using mainly Hysteresis and PPEC
- I adjusted gear mesh many times
- I tried with both a guidescope and an OAG
- I made sure everything is tight and stable
- I've recently replaced the RA/DEC boards sent by iOptron that reduce EMI
So here are my findings along with some questions. I'm hoping someone has had some experiences with these issues that could
shed some light and help me figure this out.
I will also be sharing some guidelogs throughout this thread.
Here are my findings/problems/questions:
1- During Calibration, I've noticed that the RA sometimes tends to "fall" towards the east first before responding to the west pulses.
It looks very weird and I've never had this issue before with other mounts. I tried to tighten the belt thinking maybe
it could be backlash but that didn't solve it. Adjusting gear mesh doesn't seem to solve it either unless I'm unknowingly
far from the sweet spot which I doubt.(Btw you might find in the guidelog some calibration trials that are far from dec 0
but I tried to calibrate close to dec 0 with the same results)
2- While trying PPEC, I've noticed that PHD2 sometimes fails to detect the actual worm gear period of 348 seconds, and
it tends to use values which have a 4:1 3:1 2:1 ratio. So sometimes it might detect 87s as the period, other times
it might detect it as 174 and sometimes it even surpasses the 348s mark.
3- When using the frequency analyzer in PHDlogviewer, I've noticed that there is one period, 87s, which tends to have
a very high amplitude, even higher than the worm gear and I suspect that PHD2 is not reducing this error as much as it's
reducing the worm gear PE.PEC training doesn't seem to reduce it. At first I thought maybe that was the gearbox but
after doing some research, I found out that the motor's period is aroud 115s.
Does anyone know what could the component with an 87s period be in the CEM 70? knowing that its ratio is 4:1 wrt to the
worm gear.
4- I am getting very high minmo recommendations using GA from what I was used to. To my knowledge, higher minmo is usually
recommended in bad seeing conditions, but could it also be caused by some random errors and vibrations in the mount?
I've attached some guidelogs and screenshots. The guidelogs are not very tidy, but you can check the parts with the longest guiding time for analysis as well as the multiple calibration trials I've tried.
In summary, I'm not sure if the mount has some mechanical problems, some internal play/vibrations inducing random errors
that show up from time to time which is why I need your help analysing all the data I have. I feel like the frequency
analysis will help a lot in trying to troubleshooting.