Hi Both,
Thanks for publishing it Mathis, its a good design including what most of us would want out of a companion PA system for this awesome little radio
To be clear, I'm not a KiCad user, I mainly use Altium through a license that hasn't expired yet for my own use. Its unlikely I'll have the time to make
another revision of this, but I think its good enough at the moment to be used successfully.
Matthew, thanks for the comments. See below.
1 - Could you share your circuit/values for this?
I'll read my notes over this weekend, i'll reply with some values that keeps the bias range and reduces the compensation action. The impedance through the digipot means that the current drawn through the bias network isn't the same as Jims original design. Theoretically it should be, but this circuit doesn't behave correctly across three boards. On my 1kW LDMOS amp I use a thermistor strapped across the adjustment pin of a linear regulator, that works really well.
2 - However, it increases the risk of someone putting too much power into the amp.
I know traditionally LDMOS devices are venerable to excess gate drive, the MRF101 seems to handle 3W OK if an overdrive event did occur. Zener / TVS network would be nice, but its not really essential. I used 2*430R for the shunt and 47R for the series, giving 4dB attenuation.
4 - some room for improvement to be made for 30m.
Yes, 30m does suffer slightly as does 15m. With limited GPIO expander options the filters have been designed to extend out as much as possible, it works, but it seems an unnecessary compromise just to make it work with existing software.
3- I am connecting my VNA to pin 2 of the transformer. I connect a 12 ohm resistor (per MF101 datasheet we are told the FET presents as a load impedance of 11.3–j6.4) between transformer pin 1 and GND.
In parallel with this resistor I have swept with an 82p and 220p cap. At 28 MHz with an 82p cap I see |Z| = 98. With a 220p cap I see |Z| = 54.
So with the 220p cap we see a good |Z| approx = 50 from 160m to 10m. As I said, I'm hoping I can learn something here by an explanation of your choice to replace C66 from being 220p (per Jim's design) to 82 pF.
So the figure you have there is optimised for 13.56MHz (11.3–j6.4) wereas the figure of 12.9 – j5.3 is more correct for 29MHz operation (Page 12). But that's only marginally out, yep I agree that all makes sense and computes here too. I need to perform a similar measurement here to find out why lowering the capacitance improved or "restored" the HF gain of the PA. There maybe some small signal / large signal power dependant variability happening here. As a professional, I will often use the theory to get close and then tweak the circuit values to get the desired performance, that's all I did here. As Jim pointed out earlier, the layout has longer tracks across the PCB, which is also a 4-layer stack up. In short, I don't have an exact answer, but it does work.
5- Were you able to see this directly through a jump in the bias current?
Yes, it appears to spike using a DMM on the drain as you can see the test probe is pinched into the screw terminal block. Again, does this on all three boards and it happens on the same input numbers through SparkSDR. Not tried any of the Python stuff yet.
Thanks for the input Matthew, the OP transformer change sounds interesting, although the transformer used now hardly gets warm in use. Just want to make some more QSOs and build the switcher up next, I'll post more as we go. Too many projects during these crazy times we live in. Keeping me focused though.
Jonathan G2HFR