Updated to the newest NAZE v2.0.0 version and now my quad doesn't work.

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Dr. Huett

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Apr 15, 2017, 5:46:08 PM4/15/17
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The newest version of the Naze firmware got an upgrade a few days ago (12/4/17) to v2.0.0. The default settings seemed to have been changed. I'm not exactly sure what needs to be changed "back" to make it work. I will take a closer look on Monday. Anyone who has got it working with the newest firmware like to share what settings need to be changed? 

Dr. Huett

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Apr 21, 2017, 3:31:41 PM4/21/17
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Another new firmware update v2.0.1 on 18/4/17.

I've gotten both v2.0.0 and v2.0.1 to work. 

After updating the firmware.
Configuration Tab
     - ESC/Motor Features (Box)
          - ESC Motor Protocol
               - Select from the dropdown menu PWM
     - Receiver (Box)
          - Receiver Mode
               - Select from the dropdown menu PWM RX input (one wire per channel)
Click the button Save and Reboot at the bottom of the page.

Screenshots of my configuration tab and receiver tab:





Dr. Huett

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Apr 21, 2017, 3:35:55 PM4/21/17
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If you want to get crazy you can load up the previous version of cleanflight.

Find the version that worked before at github: https://github.com/cleanflight/cleanflight-configurator/releases

1. Clone the repo to any local directory or download it as zip (be sure to unzip the folder)
2. Start Chromium or Google Chrome and go to tools -> extension
3. Check the "Developer mode" checkbox
4. Click on load unpacked extension and point it to the Cleanflight Configurator directory (for example D:/cleanflight-configurator)

When I tried this the configuration tab did not work. (The quad did though :) )
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