I I kept the SSR assembly intact, I just moved it from the front hole to the back hole on the other side.
For the power supply, I used a small piece of extruded aluminum. I mounted the aluminum to the holes that hold the leg on. And mounted the power supply to the aluminum using the existing holes in the power supply shield. I mounted the power supply as close the back wall as possible. It comes a little close to the pins on the switch, but some soldering and heat shrink tubing will eliminate any possible problems.
I used a couple of washers under the extruded aluminum, to give the back cover some room to slide into its normal position. Between the extruded aluminum and the front case.
I also powder coated my case "Harbor Freight Yellow", yeah I know, looks a lot more orange than yellow... And I powder coated the legs black (in order to powder coat the legs, I had to remove the mill coating by soaking them for about 15 minutes, in a bath of diluted muratic acid).
@Steven, @James s
@Steven I liked this Idea of placing the SSR, PCB and Terminal Strip on the Left side and then mounting the Power supply Vertical. However the Standard Bracket was broken. Even after gluing it it did not have enough strength and the PCB Blocks access to the SSR terminals. So
Here is a mount that hold everything on the left side securely without Blocking any of the connections.
The Bracket below is for the Left side I will also make a Right Side version for those people who would prefer it. I will put the STL files up on thingivers and post links here soon !
@Steven I added a notch on the outside for the back panel to slip under also the PCB is in the same place on the Left side so your cable should reach now. (you will need to make the cable come out of the left side of the Optic Assembly.)
Though you might appreciate these features :)
would really like any feed back on anything else that I should add to this thing.
Here pictures of my finished ExtrusionBot (prior to putting in the thermal insulator cloth).
I switched the legs, so that the cables could reach the controller board (now mounted on the left side).
On the back cover, I replaced the supplied power cable with the power socket from an old PC Power Supply.
I replaced the drive motor's rubber chain tensioner with an adjustable aluminum bracket.
The Spooler Motor Switch wires come off sideways instead of straight up, so they don't interfere with the power supply.
Since the hotbed on my 3D Printer is quite up to printing with ABS yet, and I currently only have ABS filament, instead of printing a bracket to hold my electronics, I fashioned one out of 2 small pieces of extruded aluminum. To give enough clearance for the screw to hold the cover on, I used a couple of 1/4 inch or so thick blocks of aluminum as standoffs.
I replaced any of the wires that came with the kit, that might require more than digital signal current, with thicker wires.
I moved the fan... The spool I have is 3 3/4 inches in radius. And that was too big to fit with the fan in the stock position. So I put the fan on the leg with the motor. This allows me to take the back cover on and off without messing with the fan.
Because my kit was missing the filament pulley and the black spooler motor spindle extension, I had to make my own versions of them.
I put a heat sink on the drive shaft motor, with mounts for a small fan (but the small fan it had was bad, so I need to replace it). I suspect if I have the chain tensioned correctly and I wait until the unit has been at the set temperature for 5 to 10 minutes before turning on the main motor, I probably won't have over-heating problems.
And just because I was in a modding mood, I leveled out the extrusion tube. I put a second fender washer on the lower mount. And on the upper mount, I trimmed down the bolt and nut and put the lock washer inside the bracket instead of between the bracket and the fender washer. These 2 little changes made the extrusion tube almost completely parallel to the front face.
This is a picture of the drive motor's heat sink.
This is a picture of the aluminum chain tensioner, that replaced the rubber piece.
These are pictures of the electronics bracket.
The PC Power Socket.
The new fan position.
Clearance around the hot extrusion tube, that will be wrapped in the insulation blanket.
Fabricated spooler motor mount and spooler motor switch assembly.
Centered Extrusion Nozzle (made it easier to get the insulating blanket around the extrusion tube).
@Steven Yaeger, Very nice work ! I am making a aluminum Heatsink for the main motor now. I looked for a hobby motor heat sink that would work but could not find one. Did you find and of the shelf heat sink that you used?
I also think that the aluminum chain tensioner is excellent as it looks like it would also help stablize the motor up and down as well as sid to side. would like to have more information on what type of stock you made it with.
was it U channel stock aluminum?
I was thinking about adding a washer to the extruder mounts to put it in the center like you have done but I think the reason it was off center was to aim it straight at the take-up roller so that the hot plastic is not bent coming out of the extruder. I guess the real answer will be if it makes good plastic filiment then it is much nicer.
on Note I did not see here is if you flip the take-up reel motor to the other side you need to reverse the polarity on the motor because it will need to turn in the opposite direction.
Very Nice work But it now makes me have lots of Questions:)
have you extruded any plastic filament?
does the aluminum heat sink work to keep the motor cool?
Is the filament holding to the +/-0.1mm tolerances?
does the Reel load up neatly? (this is my goal I cannot stand the Rats nest that most of the home grown extruders make )
I only had my Extruder running for about two day I had messed up drilling the rubber stoppers so bad that the spool would walk off the spooler.
however during that time I was able to extrude about 6feet onto a spool and after I tool it off and found that it was very good I measured it from 3.08mm to 2.98mm I was happy other than I needed the sppol to stay on more than 90 seconds.
so I have taken it apart and am doing upgrades to get it right so please let me know what works or what doesn't I will do the same as soon as I get it done I will post all the details.