Well, It's done.
I have some tweaks to do, like re-locating the powersupply, and I'd like to come up with a better mounting system for the wire. But it's cutting and my buddy is happy with the result.
I've shrunk the wire to 10 inch because for cutting EVA foam (like what is used for those mats that relieve back strain when you are in a shop) just took too much pressure on the wire.
If you remember, I was working on a motor to raise and lower the solar screen/curtain outside my windows (still in progress) and that it uses a hand crank. Well, I took that aluminum pole/crank and carefully bent it over my knee to create the arm for the cutter. Then ran the write through it, mounted the powersupply underneath, added an on/off switch, and used click butt connectors at the ends of my leads to connect to the NiCr wire. Flick the switch, and it heats up nicely in about 10 seconds and cuts well.
The click connectors are OK, but I need something better. Too much tension and they will pop off. I've left it on though for 30+ minutes and the connectors never show signs of over heating or melting (whew).
The powersupply has a small LED on it to show power. I think I'll see about figuring a way to mount that so it's visible.
And last but not least, I need to clean up the table top. I used some slick strip on the surface of the plywood. Not sure if that was a good idea or not, but to accommodate the center hole, I worked from the outsides in (not the best idea) and left a strip up the center that I need to fill in. That I'll do tomorrow.
If I can, I'll bring it by on Saturday since I can't seem to upload the video - too damn big.