i have a 5gen and only a couple weeks into using it. I'm posting this because in the past couple weeks i've been scouring the web for improvements and fixes. after 90hrs of build time, i started suffering from the extruder issues we all know about. it took 2 wk to get a replacement extruder from MBI and was ready to get back to it since the first prints were pretty amazing and i was very excited. here are some things that NOW (so far) almost 200 new extruder hours of build without ANY issue.in no order of priority:1. Filament holder- it's neat to have a filament holder built in, but the design is not great and adds a huge amount of friction that the extruder is trying to pull through. build a friction free spooler for one or more reels. i used this from thingverse, a steel rod and some hangers i found on thingverse. it's mounted under a LACK ikea shelf. i've since added a foam 'brake' to let the reels gently spool but not unwind. I'm not very concerned about moisture, not too humid here and we are burning through the filament and an inline dust cleaner.2. Leveling plate- 1.3 seems to have better leveling, but sh$@ier homing, so i leveled it in 1.3 and redid it a couple times and it thought it was still level, then backleveled to 1.2 because with 1.3 i was getting premature homulation, (thats a joke, not a slur). when people say to level your plate frequently that is not great advice, once it is leveled its leveled unless you yank on the plate or do something like punch it. i used the file attachment on this post to check the leveling, force your 5gen to print it at 10mm/sec ( am sorry i cant find attribution for it i didnt make it) adjust as necessary in small increments until you stick all the way around.3. Build surface- starting with the blue tape had some decent luck once it all was level. i also tried the purple washable elmers gluestick, which was in my opinion superior to the tape and also way cheap. the blue tape was only a 1-4 time use for me before i messed it up. the gluestick was GREAT for adhesion. it was a little messy. things popped off of it without issues. the blue tape frequently stuck to the prints and i had to then get the blue tape off the prints. i read a post somewhere when someone mentioned the PRINTINZ plates and lexan. i went straight to Home Depot and got a 8x10 piece of LEXAN for $3.97 and some scotch double sided thin tape. i taped it to my glass plate and ran the test level stl. everything stuck all the way around, GREAT ITS LEVEL and it stuck. i've since run about 25 prints on it and not had one lift up, including these few with no rafts and at .1 and .2 res.:I've ordered a plate from PRINTINZ to see the difference between it and the Lexan surface.3. Homing- i had very little luck reliably homing with 1.3, all of the first couple weeks of prints were done on 1.2 and homed fine, then the extruder pooped out. with the new extruder i've found with 1.3 it would home and think it was in place, but always many MM high. so for me i put it to 1.2 and it homes perfectly. the 5th Gen rams its hot nozzle into the print bed where i already see a deformation in the glass plate, it also then burns through your tape if you are using it. Z wont home correctly after many prints. in this homing madness i was talking to wayne at PRINTINZ (which i am not affiliated with nor do i gain any compensation-just found them this week and in a back and forth about his 5th gen plate we worked together with a german chap he was already working with on making things better for the 5th gen). here is his posting on his blog that i helped work up and test out, and i'll excerpt it if you dont want to go there.If you have tried the stock print surface or use a different surface with the Makerbot 5th Generation printer, you probably discovered that the homing sequence makes the 180°C nozzle touch your surface, slowly deforming it print after print. This makes homing less and less accurate over time. There is a work around for this problem and it's worth understanding it to take advantage of the superior capabilities of the PRINTinZ plate made for this machine.
When the machine runs its normal homing routine, just before printing, it homes in X and then Y and then raises the bed up to touch the pre-heated nozzle tip. With the PRINTinZ plate, or even blue tape with the stock glass plate, this will leave an impression and inaccurately set the Z zero after time. You can watch the homing sequence here.
This solution relies on touching off in Z against a thin metal block or other object of known thickness. Let's call that thickness Zoffset .
Start by setting the amount measured for Zoffset as a negative (-) "bedZOffset" in the Makerbot print profile in millimeters (ex. "bedZOffset": -3.0,). Place your metal object in the center of the bed and start the print cycle (be sure it will let the nozzle hit AND be seen by the LED). Try to clean off any extruded filament from the nozzle tip before it touches the metal block. Let the homing process complete its 2 part homing process. When the printer returns to the "FINAL HEATING" position, remove the metal block from the bed.
An important point to remember is that the offset does NOT affect the initial anchor. This will be much too high and extrude in the air - just like the machine measured it. The offset starts to take effect AFTER the anchor is printed. Wait for the real print to start. Note also that you may have to adjust the value entered for Zoffset slightly to get good results. This method reportedly works well using firmware version 1.2, and with 1.3.0.131 (as of 8/28/2014).
Special thanks to Patrick Kapsch and David Ballard for developing this solution.That's my Lexan build plate and a close to 3mm aluminum stock. i have -3.2 as my zbedoffset and it is right on. HOMING SOLVED! 20 or so prints and not one off.4. Custom Profiles- the default settings for Mister 5th gen are good for the novice, but offer very neutered control of the printer forcing you into custom profile land. here are some things that i change in making custom profiles that work without making the extruder work too hard and for me improve print quality, a fast sh**ty print isn't much good to most:"layerHeight": 0.20,sets .1 for high, .2 for std, .3 for low"bedZOffset": 0.0,sets the reverse offset if you are using a 'homing block' this is set in mm so get a caliper and measure your offset object and make it negative, for me it's: "bedZOffset": -3.2,"doDynamicSpeed": true,this slows down the extruder on sharp turns, i've seen TRUE to give some finer results but can give buldging sometimes on slow down parts"numberOfShells": 2,sets the # of shells you want"infillDensity": 0.1,sets the % of infill, ex. .1 is 10% 1.0 is 100%"doRaft": false,if you do or dont want a raft, i am now mostly not using a raft with the Lexan even for small vertical objects with little surface like these at .1 resolution:"doSupport": false,if you want support TRUE OR FALSEI SET THESE ON ALL PROFILES- ive found that the default 90mm/s is way too fast for the extruder- some may have better luck, but slowing things down is helping me.-----first layer is important if not printing with raft, you have to go slow at finer resolutions on layer 1 or it just wont stick in my experience."firstlayer": {"feedrate": 10,"infill": {"feedrate": 70,"insets": {"feedrate": 70,5 EXPERIMENTAL- Extruder Preventative Measures- in one of the above photos you see a little green thing on my extruder. a friend made this thing and we are testing it out. so far without any ill effects, zero air prints or under extrusions, no 'CLICKING' or 'FILAMENT JAM'. i've put almost 200hrs on this new extruder with this mod and it could be a placebo, but i know my 5GEN is running night and day! i will post info about this if he's ok with it.that took about 2hrs to put together and if that 2hrs helps ANY 1 5GEN owner, it is worth it. i considered posting to many different posts but it made sense to compile this- i believe it is STICKY worthy.here's more of those Corkasauruses you saw starting out earlier, still sticking!once again i am a new user who just got this device and i feel much happier about this purchase than i did 2wks ago when it quit working...If you feel i've given any inaccurate or harmful advice let me know kindly.if you have any questions feel free to contact me, but to my real email, i may not check this thread vigilantly- ALSO if you got this far, congratulations and thank you- i'm not just printing funny little items- we've prototyped some really big 35hr build items that you should see on the shelves in a couple mos!daveDavid C. Ballard
Principal, LABTOPIA FARMS
dave at labtopiafarms.com
toby i am still having a hard time figuring how to edit, it is not an option, not a big deal. and ryan, thanks i think it should be a sticky, there are only 8 right now and i really think this one is valuable
i have a 5gen and only a couple weeks into using it. I'm posting this because in the past couple weeks i've been scouring the web for improvements and fixes. after 90hrs of build time, i started suffering from the extruder issues we all know about. it took 2 wk to get a replacement extruder from MBI and was ready to get back to it since the first prints were pretty amazing and i was very excited. here are some things that NOW (so far) almost 200 new extruder hours of build without ANY issue.in no order of priority:1. Filament holder- it's neat to have a filament holder built in, but the design is not great and adds a huge amount of friction that the extruder is trying to pull through. build a friction free spooler for one or more reels. i used this from thingverse, a steel rod and some hangers i found on thingverse. it's mounted under a LACK ikea shelf. i've since added a foam 'brake' to let the reels gently spool but not unwind. I'm not very concerned about moisture, not too humid here and we are burning through the filament and an inline dust cleaner.
This involves adding a small reservoir on top of your extruder that has a cotton ball in it (good for getting dust off filament) but also has a couple drops of canola oil in it. this seems to keep the extruder from 'CLICKING' and failing to draw the filament through causing 'FILAMENT JAM' or just air prints. you should read the whole thread and understand it but the broad points include, printing the cut and top, adding a cotton ball and some drops of canola feed your filament through and load it into mister extruder. do not go crazy with the oil, just a couple drops does the trick.this is the last thing i wanted to post to my thread. it may be placebo, but i know my extruder has been working longer than 2 times the first without issue, about 200hrs of new prints. attached are the stl for the 2 files. print them .3 mm 2 shell/100infill (at least thats what i did), face them both as they should be to the ground.read below....
Michael Carmenaty Aug 14
Hi Guys!!!
Well after having the MakerBot for about 2 months its been nothing but headaches.
First week I had the printer was working perfectly. Then it all went down hill from that point on.
I think there sample prints are small and not complex so I'm guessing that's why the prints came out prefect.
Anyways Problems from the beginning
- MakerBot Desk Top was not working correctly, I could not get any part to export the file so I can save it to a USB and print that way.
- MakerBot Service is Horrible. I did get some help but it would take them a week to 2 weeks to get back to me.
- When I tried printing large parts that would almost cover the entire build plate. The corners would peel up making the part not flat/straight
After I had fixed all the issues above. I said: finally I should be ok now to print usable parts here at work. NOPE!!!!
The biggest problem now I have is the feeding of the filament.
I don't know if the new firmware for the printer has messed up something in the programming of the smart extruder.
First I was getting a small jam were the extruder started knocking and no Filament was coming out. So I just did the unload process and reloaded the filament.
Filament was coming out of the nozzle. So I continued my print and monitor it for the first couple of minutes. It was printing ok, left it alone came back the next
morning print was half way done. DAAAM!!!
I was searching on the web and found that most people have replace there smart extruder for a new on from MB. But what surprised me was that they had replaced it 3 time?!?!
I said the hell with that so I opened the extruder found lots for grinned down filament inside. So I just went head and cleaned it up. Its very simple to open just need to be gentle not to brake the tabs There was a filaments inside that was not letting the new filament feed through. So i just just cut it. Put everything back together.
Ok so loaded the new filament. Success came out the nozzle. So i did a quick print to see if everything was ok. It was printing fine. BUT....
5 minutes into the print the knocking came back AGAIN! it was not feeding Correctly
So I did this about 6 times open, clean, print, fail. I said what is going on contact MB. Still waiting on there reply
So did more research. Found out some one suggested Olive oil or baby oil on the Filament.
It makes sense to lubricate the filament that way when it enter the heating element and nozzle the PLA will not stick to the walls.
I figure Ill try this one more time if this dose not work. I'm sending it back. SOB!!! its worked.
But I think this is a temporary solution maybe if MB does another Firmware. This issue might be fixed just on firmware alone.
OK so this is how I started my discovery and ended up with something everyone with a Makerbot 5th Gen can use if they are running into this problem
So I got Air tool oil this is what i had at the moment just so i can try it out to see if it works.
I put a small amount of oil on a paper towel. I exposed the filament from the guide tube and wrapped it around filament.
Then I got a paperclip just to hold the paper towel around the filament.
So as the filament is being fed through the Smart Extruder its also getting a thin coat of oil.
Ran a test print which was the Bracelet sample. SUCCESS!!!
No skipping, No knocking, No Ghost or air print.
So I went ahead and designed the oil reservoir
The Idea here is this will sit on top of the extruder were the filament is fed through.
I printed these out. Using the MakerBot when i had the paper towel :)
Here Is a quick test fit. Perfect!!
So no just need to add cotton inside the reservoir & then add a couple of drops off baby oil
No need to fill the entire reservoir of oil. you don't want it to leak through the bottom and into the extruder.
The cotton will add like a wick keeping the oil inside
Here is the Final look :)
So now if you hear the knocking start to come back. just add a couple of drops into these slots.
No need to take the cap off. I used this bottle and filled it up with baby oil
Well hope this will help anyone out there that having this issue. I figure I make this topic. The MakerBot groups have helped me a lot. Some of the tips and trick I used to get my makerbot going were form these These groups
Sucks MBI support sucks. If they would make there support stronger. They could be one of the best companies out there.
I will put the files on for this oil reservoir I made on http://www.thingiverse.com
I anyone want the STL files let me know i will be glad to give them to you.
Here is more information on how PLA works.
http://www.matterhackers.com/articles/how-to-succeed-when-printing-in-plaagain i haven't had any issue since using this- only that my prints have been reliable. this has worked fine for me and printing error free so far well beyond when the first extruder jacked up. here are some trivial prints- i cant post some for client reasons, but these are fun and show .1 .2 .3 all with this 'lube' method and on lexan:
Use at your own risk but i have not had anything negative using this mod so far...cheers!dave
...<a style="margin-right: 1em; margin-left: 1em;" onmousedown="this.href='https://lh5.googleusercontent.com/-TIAY3XUSGhs/VAE1em_9E0I/AAAAAAAAh4s/vQK98TrDUAo/s1600/IMG_20140824_123443_563.jpg';return true;" onclick="this.href='https://lh5.googleusercontent.com/-TIAY3XUSGhs/VAE1em_9E0I/AAAAAAAAh4s/vQK98TrDUAo/s1600/IMG_20140824_123443_563.jpg';return true;" href="https://lh5.googleusercontent.com/-TIAY3XUSGhs/VAE1em_9E0I/AAAAAAAAh4s/vQK98TrDUAo/s1600/IMG_20140824_
hi wanted to share some more prints. like i mentioned after moding my operation of the machine detailed above it is really good as far as i am concerned. i have not had a print failure or any extruder issue. i give very much thanks to michael Carmenaty for posting his solution- it works great for me! i am upset about the mb software that is neutered and you have to make a million profiles to print, just for a quick print with zoffset which i do to protect my plate i should just have a tab in there to do that. also the slicer is not great but its all i got as an option...also i made another $250 today printing some architectural stuff that shapeways quoted as 325 and 1 wk turnaround...i have a happy client. and the clear is way oozier than anything else i've printed...thanks! dave
You paid nearly $3k and unfortunately are not even getting $1k printer output.
On 11/09/2014, 10:17 PM, David Ballard wrote:
> howdy jetguy you didnt ask how this was printed... this was printed at
> .3mm res so it will be rough.
It's not the layer roughness we're referring to: it's the vertical banding.
It's the "scalloped" bands that run vertically. Bad acceleration performance leads to unsmooth movement that causes that.
I also see a few other issues in your other print. Mind you, these occur with other printers, too. But a well running printer would not have these issues (or it would be less noticeable).
for vertical banding, you mean where it starts each layer and leave that thing there? yes i am not a fan...
On Friday, September 12, 2014 1:37:42 AM UTC-4, dnewman wrote:
Really interesting, thanks for sharing! We've had a lot of lifting/warping issues so I'm going to check out your tip on the lexan and see if that helps.
It still cracks me up that MB desktop won't let you change things like forcing you to use a raft or graying out other options just cause you didn't pay the extra $1500 for their higher end machines. Glad I don't have to deal with that joke anymore